Maximized X

Submitted by xjcdadmin on Thu, 06/14/2012 - 23:18

The Maxim X tank is a little on the small side. So when I had to repair a big dent as part of a restoration project anyway, I thought I'd address the size too. I didn't want to ruin the classic lines of the X tank, so after much debate, I decided to widen it a few inches, leaving the profile intact. The first step was to layout the planned cut with narrow masking tape. Normally used for things like pinstriping, it follows curves quite nicely. 01-layout_cuts-800.jpg

Once I was satisfied, I did the old Hardy Boys pencil trick on some paper to make a mask for the filler metal. Then I shifted the paper by the amount I wanted to widen the tank and did it again. Repeat for other side. 02-create_template-800.jpg

An old car hood was just the right gauge for the tank. The paper was cut out then laid flat to mark the metal... 03-cut-sheet-metal-800.jpg

... and the tank was laid open along the cut line. I left a tiny bit of metal intact at the narrow point to ensure alignment. 04-cut_on_dotted_line-800.jpg

Once the filler strip was cut, it had to be curved to fit the curve of the tank. It is very easy to confuse which end is up at this stage! 05-filler_strip-800.jpg

The edges were then treated with a pneumatic panel raising tool to recess the underlap. 06-recess_edges-800.jpg

It took a lot of clamps to position things exactly right. 07-forest_of_clamps-800.jpg

Once in position, the filler was tacked every few inches to keep it there while the other side was fitted into place. 08-tack_in_place-800.jpg

Ok, how do you clamp the other side? A ratchet strap or two did the job quite admirably: 09-clamp_outer_side-800.jpg

Not quite perfectly though. Welding distorts metal, especially thin metal. To close this gap a small tab was first tacked to the filler strip... 10-fix_gap-800.jpg

Then the temporary tab was pulled with pliers to close the gap and things were tacked in place before the tab was ground off. 11-pull_tab_to_close-800.jpg

The seam was then welded between the tacks, running short beads alternately on opposite sides and ends to minimize distortion. Here is a before-and-after comparison of the widened side and the original. Of course, the entire process was then repeated on the opposite side. 12-first_side_done-800.jpg

The welds were pressure tested to 15psi. I'd love to say my welds were perfect, but I'd be lying. Soap and water solution pinpointed the pinpoints, which were marked, ground and re-welded. Once it was pressure-tight, the tank was de-rusted and coated with POR-15 to preserve the interior until the end of time. I hope. Then it's all down to standard bodywork to smooth things out. "Kitty hair" fiberglass went down first, followed by bondo. Sand and repeat, time and again. Compound curves are tricky!

13-skim_coats_over_fiberglass_layer-800.jpg

And here it is, ready for primer and paint: 14-still_more_layers-800.jpg

Total increase in width: 2-1/2". Should add approximately 2 litres to the capacity. tafn dv UPDATE: Here it is painted and mounted on the bike. No difference in profile:
15-painted_profile.jpg

But look at it from above:

16-painted-top.jpg